Abstract
Slicing fully mechanized caving mining is a standard high-efficiency mining method for ultrathick coal seams. However, the effectiveness of gas control has accentuated the difficulty in fully mechanized top coal caving of low-permeability ultrathick coal seams. This study focused on mining the No. 9-15 coal in Liuhuanggou Coal Mine, Xinjiang Province, China. To this aim, the results of theoretical analyses and field tests were combined to explore a comprehensive gas control method for fully mechanized caving of low-permeability ultrathick coal seams. The No. (9-15)06 panel was a top-slicing panel of the No. 9-15 coal with a mining height of 9 m. Gas analysis results revealed that gas emissions in the No. (9-15)06 panel are mainly sourced from the coal wall, caving top coal, goaf, and neighboring coal seams. Based on gas source separation, a comprehensive gas control method was proposed. The proposed method was based on the combination of gas predrainage alongside the coal seam, high-position drilling on the top, preburial of pipes in the goaf, and pressure-balancing ventilation. The permeability and gas predrainage were enhanced by hydraulic fracturing in low-permeability coal seams. According to the characterizations of coal seam and crustal stress distribution, the arrangement of the boreholes and backward-segmented fracturing technology were designed. From the field results, the coal seam presented a remarkable prefracturing under hydraulic fracturing. Besides, the mean gas predrainage from the boreholes was enhanced by four times compared to the prehydraulic fracturing state. Finally, using the proposed comprehensive control method based on the gas sources, field tests were performed in the No. (9-15)06 panel. The measured results demonstrated that gas concentration in the return airflow is fluctuated within a range of 0.05% to 0.35%. The proposed gas control method can provide an insightful reference for other similar projects.
1. Introduction
Slicing fully mechanized mining is a high-efficiency mining method for ultrathick seams in China. However, most of China’s coal fields include high gas and low permeability [1, 2]. Ultrathick seams with low permeability are commonly deficient in gas predrainage. When using the fully mechanized mining method, a significant amount of gas is emitted from coal seams. The high concentration and accumulation of gas in fractures can easily trigger a formidable accident such as a gas explosion in the overlying strata of the goaf and threaten production safety in the mines [3, 4]. Numerous attempts have been made to develop useful gas drainage and discharge methods and achieve adequate gas control by the fully mechanized mining of low-permeability ultrathick coal seams.
Fan and Wang focused on fully mechanized mining of ultrathick mines in Tashan Mine and proposed the gas in the goaf can be controlled by combining vertical surface drilling and high-position gas drainage roadways [5]. However, for the mines with great burial depth, the cost of gas drainage by drilling a significant number of vertical holes is high. According to the characteristics of longwall coal mining in Australia, Guo et al. projected a gas drainage and discharge method for the goaf using horizontal drilling [6]. They exhibited a good drilling operation in the construction of the roof fracturing zone. Furthermore, Zhang et al. examined the development rules for the roof fracturing zone when using high-dipping longwall coal caving and the related effect on gas drainage [7]. They designed an optimal construction layer during high-position drilling for gas drainage and discharged from the No. 704 panel of Baojishan Mine [7]. Moreover, Liu addressed gas accumulation at the upper corner of the goaf in a fully mechanized panel for tilted ultrathick coal seams [8]. This technique was successfully applied in Wudong Mine [8] by preburying gas drainage and discharge pipes in the goaf.
In previous studies, a straight-line construction was performed for gas drainage in surface and underground drilling operations. Recently, new means of gas drainage are provided by directional drilling in coal mines. In this regard, boreholes can be drilled in coal seams along with a preset direction [9]. Taking Daning Mine, Shanzi, China, as an example, Lu et al. carried out the directional drilling in coal seams for gas predrainage and achieved favorable results [10]. Li et al. proposed a new inverse -type drilling mode for gas drainage and discharge and realized the gas comprehensively controlled through passing the caving zone, fracture zone, and coal seams in the working face [11]. In contrast to traditional drilling, the directional drilling of the coal seam exhibits a series of advantages, including strong adaptability, high drilling proportion, and good efficiency of gas drainage. Although these advantages are appropriate to gas control in directional drilling of coal seams, they should be pretty permeable.
For low-permeability coal seams, drilling alongside the coal seam has a poor gas drainage performance; therefore, some fracturing techniques are necessary for prefracturing in coal seams and enhancing their permeability. Deep-hole loosening blasting is a common prefracturing technique in coal seams [12, 13]. However, this technique has certain shortcomings. The dynamic shock wave produced in the deep-hole blasting can easily damage the surrounding rocks in the tunnel and lead to more difficulty controlling the rock deformation. Also, unreasonable deep-hole blasting schemes trigger numerous accidents such as gas explosions and coal and gas outbursts. Many scholars performed numerous studies and explored some methods such as hydraulic fracturing for enhancing the permeability in coal seams [14–16]. Hydraulic fracturing refers to drilling boreholes in the coal seams, followed by generating fractures through high-pressure water as a medium. In these enclosed boreholes, hydraulic pressure is utilized to overcome the tensile strength of surrounding rocks [17]. After hydraulic fracturing, the initial fractures are formed in the coal, and numerous secondary fractures are produced [17]. Gas transport channels can be increased while promoting the desorption of adsorbed gas, thereby leading an increase in coal permeability and range [18, 19]. In recent years, some scholars developed directional hydraulic fracturing and pulsed hydraulic fracturing techniques [20, 21].
Moreover, the effective gas control has always remained a technical difficulty in the fully mechanized mining of low-permeability ultrathick coal seams. As described earlier, some scholars have proposed numerous gas control methods and attained favorable results. In the fully mechanized mining of low-permeability ultrathick coal seams, gas has various sources and is significantly challenging to control. Currently, one method addressing the control of multisource gas in the working face is lacking. This study focused on mining the No. 9-15 coal in Liuhuanggou Coal Mine, Xinjiang Province, China, and innovatively proposed a comprehensive gas control method. It is based on the gas emission analysis in which gas predrainage alongside the coal seam, high-position drilling on the top, preburial of pipes in the goaf, and pressure-balancing ventilation are combined. Considering the poor gas predrainage effect for low-permeability coal seams, the permeability and gas predrainage are enhanced by hydraulic fracturing. In this regard, a scheme of hydraulic fracturing is designed, and the performance of the prefracturing and permeability enhancement in the coal seams is verified through field measurements. Lastly, the proposed source-separation comprehensive gas control method’s effectiveness and reliability are validated using long-term field tests. The proposed gas control concept and methods can provide a valuable reference for other similar projects.
2. Case Study
2.1. Mining and Geological Conditions
As shown in Figure 1, the No. 9-15 coal seam, with a mean thickness of 32.94 m and a mean inclination angle of 24°, is the primary mineable coal seams in Liuhuanggou Coal Mine. The coal seam has excellent hardness and undeveloped fractures. Also, the measured gas content and gas pressure in the No. 9-15 coal seam were 3.85 m3/t and 0.5 MPa, respectively. Besides, the permeability coefficient ranged from 0.011814 to 0.061668 m2/MPa2 d, and the attenuation coefficient of gas flow was 1.03-1.28 d-1 in the borehole, suggesting a low-permeability coal seam.

No. 7 and No. 4-5 coal seams were also located above the No. 9-15 coal seam with mean thicknesses of 2.31 m and 7.18 m, respectively. Specifically, the No. 7 coal seam was unrecoverable. The gas content in No. 7 and No. 4-5 coal seams was 4.14 m3/t and 3.5 m3/t, respectively. The distance between No. 4-5 and No. 7 coal seams was 1.85 m, while the distance between No. 7 and No. 9-15 coal seams was 20.95 m. As illustrated in Figure 2, the roof strata of the No. 9-15 coal seam are mainly composed of siltstones and mudstones.

As an operating background in this study, the No. (9-15)06 panel was selected, 60 m away from the No (9-15)04 goaf. North of the (9-15)06 panel is the area of unmined coal. The No. (4-5)04 goaf is located on the inclined top of the north part, and the No. (4-5)02 goaf is right above the No. (9-15)06 panel. The tailgate in the No. (9-15)06 panel is inside staggered the tailgate in the No. (4-5)02 panel with a distance of 23 m, while the headgate in the No. (9-15)06 panel is inside staggered the headgate in the No. (4-5)02 panel with a distance of 11 m. A slicing mining method was used for the No. 9-15 coal seam. In the No. (9-15)06 panel, a fully mechanized longwall caving method was used to top-slicing the No. 9-15 coal, with a mining height of 9 m and a mechanized mining height of 3 m. The strike length and inclined length of the working face were 1045 m and 100 m, respectively.
2.2. Coal Seam Mechanical Parameters
To measure the related mechanical parameters of the No. 9-15 coal seam, the No. 9-15 coal samples were collected from the tailgate. Because of the significant sample thickness, coal samples were sliced into three layers: the upper, middle, and lower slices. Coal samples were processed into standard cylindrical specimens with different sizes (e.g., and ). Then, an MTS815 electrohydraulic servo rock tester was used to perform uniaxial compressive, triaxial compressive, and Brazilian disk splitting tests. The due parameters were then acquired on the standard samples, including uniaxial compressive strength (), tensile strength (), elasticity modulus (), Poisson’s ratio (), cohesive force (), and internal friction angle (). Each test was repeated five times, and then the results were averaged. Table 1 lists the mechanical parameters of the No. 9-15 coal seam. The mean uniaxial compressive strength of the No. 9-15 coal was 35.35 MPa, suggesting excellent coal seam hardness. Owing to poor permeability, gas predrainage performance on the coal seam was far from ideal. During mining in the No. (9-15)06 panel, gas control was crucial.
2.3. In Situ Measurement of Crustal Stress
To gain an in-depth knowledge of the crustal stress distribution in the Liuhuanggou Mine, in situ measurements were performed. The accuracy of in situ measurement was related to selected methods and sensors. As the stress relief method, a CSIRO hollow inclusion stress gauge was used to possess numerous advantages, including the accuracy, reasonable distribution of numerous strain gauges, and a wide application range. The measuring points should be selected far from the areas with complex geological structures and significant mining effects on this subject. Figure 3 shows five measuring points of crustal stress selected in this study. Also, in situ stress measurement points of crustal stress and borehole layout parameters are listed in Table 2. Drilling depth ranges from 10 m to 12.8 m with dominant lithology between fine sandstone and siltstone. Besides, Figure 4 displays the in situ crustal stress measurement results in Liuhuanggou Mine, in which , , and denote the maximum horizontal stress, the minimum horizontal stress, and the principal vertical stress, respectively. The dominant azimuth angle and direction of and were 230° and 140°, respectively. Figure 4 shows the crustal stress direction at each measuring point.


Moreover, Figure 5 illustrates the stress field in Liuhuanggou Mine that . As shown in Figure 5, vertical stress dominates the crustal stress field, and various principal stresses increase with increasing burial depth. As a result, vertical stress was slightly smaller than the weight of the overlying strata per unit area. Based on the method of least squares regression (), the following equations were written between various main principal stresses and burial depth ().

2.4. Analysis of Gas Sources in the No. (9-15)06 Panel
Many scholars believe that gas emission sources in the working face mining are coal walls, fallen coal, goaf, and neighboring coal seams [22]. Four main gas emission sources were identified in the No. (9-15)06 working face by analyzing the arrangement and surrounding mining conditions.
2.4.1. Gas Emission Quantity from Coal Walls ()
When the working face was to be moved forward, fresh coal walls were exposed to the air. Then, the pressure balance was broken after reliving the rock pressure. Due to a gas pressure gradient in the coal, gas was emitted through coal fractures towards the working face.
2.4.2. Gas Emission Quantity from Top Coal Caving ()
Before caving the top coal in the working face, the top coal was first fully broken under supporting pressure. The original gas pressure balance in the coal seam was then broken during the crushing of the top coal. Hence, the adsorbed gas in the coal seam was converted into a stable state of free gas and then emitted into the working face during top coal caving.
2.4.3. Gas Emission Quantity from the Goaf ()
Using the fully mechanized caving method, the recovery ratio in the No. (9-15)06 panel was about 85%, and a significant amount of coal would be left in the goaf. Therefore, gas from the unmined coal was the main source of the emitted gas in the goaf. Also, the top layer mining in the No. 9-15 coal seam affected the bottom coal seam mining by generating numerous fractures and emitting a significant amount of gas.
2.4.4. Gas Emission Quantity from the Neighboring Coal Seams ()
As shown in Figure 2, the No. 7 and No. 4-5 coal seams locate right above the No. 9-15 coal with a distance of 20.95 m and 22.8 m, respectively, and include a high content of gas. After mining the No. (9-15)06 panel, the No. 7 and No. 4-5 coal seams were located in the roof caving zone, in which a connection was made between the No. (9-15)06 panel and the No. (4-5)02 goaf. Besides, the gas emitted from the No. 7 and No. 4-5 coal seams was accumulated in the overlying strata of the goaf in the No. (9-15)06 panel.
To conclude, the total gas emission () from the No. (9-15)06 panel equals the sum of the gas emission from the above sources, i.e., . and can be lowered by gas predrainage alongside the coal seams [23]. The gas from latter two sources accumulated in fractures in the overlying goaf strata. As a result of this accumulation, the friction in fractures of overlying strata quickly triggers a gas explosion in the goaf and threatens the production safety in the working face. Therefore, effective measures are required for drainage or dilution for the gas accumulated on the top of the goaf (i.e., ).
3. Increasing the Permeability of Coal Seam by Hydraulic Fracturing
From the No. 9-15 coal seam, the performance of gas predrainage was weak due to high strength and poor permeability. Therefore, prefracturing was first performed on the coal seam to enhance the permeability by hydraulic fracturing and improve the coal seam’s gas predrainage effect.
3.1. Crack Initiation Pressure
Crack initiation pressure refers to the maximum water pressure during hydraulic fracturing. Numerous factors affect the initiation pressure, including burial depth of the coal seam, crustal stress, coal mechanical properties, and original cracks. According to the hydraulic fracturing theory [14, 24–26], tensile cracks dominate the hydraulic fracturing process. Under the action of water pressure in the boreholes and the crustal stress field, when the tensile stress on the tip of the cracks exceeds the tensile strength , cracks develop gradually. The initiation pressure can be estimated (Equation (2)) by ignoring the water seepage effect from the boreholes on the surrounding media [26]: where and denote the maximum and minimum principal stresses, respectively, and denotes the coal tensile strength.
Besides, gas pressure significantly affects crack initiation and propagation under hydraulic fracturing [27]. Based on statistics from a large number of coal mines in China, Li et al. carried out a regression analysis and determined the following relationship between crack initiation pressure , burial depth of the coal seam , and gas pressure [19]:
According to the minimum pressure principle, the minimum value between and was selected as the initiation pressure of the coal seam ():
In this study, the mean burial depth of the working face was approximately 420 m, the mean unit weight of the overlying strata was 23 kN/m3, and the gas pressure of the coal seam was 0.5 MPa. Also, the maximum and minimum principal stresses in the study area were 10.54 MPa and 6.34 MPa, respectively. From Table 1, the average tensile strength of the No. 9-15 coal was 1.97 MPa. and equal 10.45 MPa and 10.74 MPa, respectively. Therefore, is10.45 MPa.
3.2. Enhancing Coal Seam Permeability by Hydraulic Fracturing
3.2.1. Arrangement of Hydraulic Fracturing Boreholes
The spatial positions of the hydraulic fracturing and high-position gas drainage in boreholes on the roof of the working face were analyzed to avoid damages to gas drainage boreholes. This analysis was based on geological and engineering conditions of the No. (9-15)06 panel and coal seam characteristics. Figure 6 shows an arrangement of the hydraulic fracturing in boreholes. A set of boreholes with a diameter of 75 mm were arranged on the inner sides of the tailgate and headgate. The first group of boreholes was arranged 15 m from the set-up room of the No. (9-15)06 panel, and the interval between every two groups of boreholes is 8 m. Table 3 lists the detailed parameters of boreholes.

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3.2.2. Main Equipment
Many field equipment sets are used for hydraulic fracturing, including a high-pressure water injection pump, water tank, flow controller, pressure gauge, and high-pressure water pipe. The maximum pressure of the water injection pump was 35 MPa, and the water flow velocity was 200 L/min.
3.2.3. Sealing of Boreholes
Borehole sealing is a critical make-or-break step that determines the effectiveness of hydraulic fracturing. At present, cement and other particular hole packers were used for sealing [19]. The latter was used in the present field test. Under high-pressure water, the rubber gasket was compressed, then expanded radially in the hole packer, and reached the inner wall of the hole to achieve a seal. The use of this method provided a high sealing efficiency with a simple operating process in boreholes. However, this process sets high requirements on the boreholes, such as the high construction quality and the smooth borehole wall.
3.2.4. Fracturing Technology
Spatial propagation of hydraulic fractures directly affects the permeability enhancement of coal seams. The hydraulic fractures are always propagated parallel to the maximum principal stress and perpendicular to the minimum principal stress [17, 28–30].
According to in situ measurement results, the vertical stress was dominated the crustal stress in Liuhuanggou Mine. The dominant angle of the minimum horizontal stress was 140°. The angle between the dominant direction of the minimum horizontal stress and the gate axis of the panel was about 84°. Hydraulic fractures are most likely to propagate radially from the borehole; therefore, a backward-segmented fracturing technology was adopted to enhance hydraulic fracturing performance. Figure 7 illustrates the present borehole sealing method. Two-hole packers were connected in series, and the spacing distance between them (denoted as ) was the sectional fracturing length. In this study, equals 8-10 m. As shown in Figure 7, the initiation pressure of valve in hole packer A equals in hole sealer B, and both are smaller than the initiation pressure of valve C. Thus, the fracturing and sealing of local borehole can be achieved.

3.3. Verification of Permeability Enhancement of the Coal Seam via Hydraulic Fracturing
To evaluate the enhancement of permeability in the coal seam by the hydraulic fracturing, the following two methods were used for the accuracy: borescope examination and borehole gas emission quantity measurement.
3.3.1. Borescope Examination
A stratum detector was employed for examining fracturing results in the borehole before and after the hydraulic fracturing. This study emphasizes both crack initiation and propagation behaviors in the borehole. Figure 8 shows the distribution of cracks in the borehole before and after the hydraulic fracturing. The inner wall of the initial borehole was complete in shape, while few original cracks were found in the borehole. After the hydraulic fracturing, cracks were propagated radially or in a spiral pattern from the borehole wall. This result correlates with the distribution of crustal stress in the test region, which was consistent with the predicted results as described above. In conclusion, the coal seam showed satisfactory prefracturing performance.

3.3.2. Measurement of Gas Emission Quantity from the Borehole
Before and after the hydraulic fracturing, gas predrainage flows were monitored using an orifice plate flow meter [31]. The gas flow in the borehole can be calculated as Equations (5) and (6): where and denote the flow of drained gas mixture and pure gas, respectively, in m3/min. denotes gas concentration (%) in the gas mixture, and is the actual characteristic coefficient of orifice flow. is the correction coefficient of gas concentration (), and is the difference between the measured pressure (mmH2O) of the front and rear ends in the hole plate. denotes the correction coefficient of gas pressure (). 760 is the standard atmospheric pressure. denotes the measured absolute pressure (mmHg) at the windward end of the hole plate. denotes the correction coefficient of temperature (). 293 is the standard absolute temperature (°C). Also, denotes the temperature (°C) at the measuring point in the gas pipe.
Furthermore, the U-shaped differential pressure gauge readings were obtained and substituted into Equations (5) and (6) to calculate the exhausted gas mixture and pure gas. Figure 9 presents a plot of the results from the various rules of gas predrainage quality in the borehole before and after the hydraulic fracturing. After implementing hydraulic fracturing, the mean gas predrainage quantity from the borehole was enhanced by nearly four times the original value. Besides, in low-permeability hard coals, fractures were propagated around the borehole after the hydraulic fracturing. Therefore, the permeability of the surrounding coal seams was increased, and the performance of gas predrainage was remarkably improved.

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4. Comprehensive Gas Control Based on Sources
A comprehensive gas control method was proposed by analyzing four main gas emission sources in the No. (9-15)06 panel (Figure 10). Before mining in the panel, the quantity of and was lowered by performing gas predrainage in the coal seam. During the working face mining, the gas was accumulated in the caving zone. In doing so, the fracture zone () was discharged through high-position boreholes on the roof. Meanwhile, drainage pipes were buried along with the tailgate in the panel to address the gas accumulation in the upper corner. Also, pressure-balancing ventilation was implemented during the working face mining. To prevent the air leakage and gas emission in the goaf, the difference between the measured pressures of two gate roads was reduced by adjusting the ventilation parameters.

4.1. Gas Predrainage in the Coal Seam
Hydraulic fractured boreholes were also used as gas predrainage holes before the working face mining for the gas predrainage in the coal seam (Figure 11). Accordingly, two purposes were obtained by predrainage holes: the enhancement of gas predrainage and reduction of construction volume.

The system of gas predrainage in the coal seam mainly consists of drainage pipe, filter pipe, collecting pipe, and hole-sealing materials (Figure 11). The auxiliary devices include the flow meter, the concentration meter, and the pressure gauges. Also, metal sleeves with a diameter of 40 mm and a wall thickness of 3 mm were put in each fractured borehole, and small-diameter holes were arranged at one of the sleeves’ ends. Two sections of the sleeves were arranged around each borehole, and each section was 3-4 m in length. After installation of the sleeves, boreholes were sealed using polyurethane (PU). It is important to note that hole-sealing depth should not exceed the burial depth of the gas drainage pipe in the borehole. Lastly, the sleeves were connected with the gas drainage header pipes, providing a negative pressure of 25 kPa.
4.2. Drainage of Gas from the Caving Zone via High-Position Boreholes
Gas emitted from pressure relief in the coal seam floor was an essential gas source in the mining panel. After the working face mining, the overlying strata underwent fracturing and formed the bent subsidence zone, the fracture zone, and the caving zone [32–35]. Meanwhile, many layered and vertical fractures were produced [36, 37], and gas was accumulated in these regions. The accumulation of emitted gas from No. 4-5 coal, No. 7 coal, and No. 9-15 coal increased the gas accidents. Therefore, based on gas predrainage in the coal seam before the mining, long-strike holes were drilled in the high-position drilling site on the roof. It was performed for discharging the gas accumulated in the caving and fracture zones during working face mining (Figure 12). The high-position drilling site was located in the tailgate of the No. (9-15)06 panel. Drilling sites were set at an interval of 60 m. In each drilling site, 16 long boreholes in 4 rows were arranged alongside the strike of the coal seam in a fan-shaped distribution.

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4.3. Gas Drainage at the Upper Corner of the Panel
The gas produced in pressure relief from the floor can rush into the goaf and enter the upper corner, resulting in an abundance of gas in the corner. To avoid the above problem, gas drainage pipes were buried at the air return corner on the top of the goaf during working face mining (Figure 12).
4.4. Pressure-Balancing Ventilation for Reducing Air Leakage in the Goaf
The air supply is generally increased for diluting the gas concentration in the return airflow for the panels with U-shaped ventilation. It is an incorrect practice. Increasing the quantity of air supply in the panel blindly can increase the difference in the measured air pressure between the goaf and the panel and air leakage in the panel, leading to an increase in gas emission in the goaf and gas concentration in the panel return airflow [38]. On that basis, pressure-balancing ventilation was adopted to reduce the difference in the measured pressure between two sides in the air intake and return roadways. By the way, the distribution of the ventilation system’s pressure was changed [39]. Accordingly, the air leakage can be lowered to inhibit gas emissions from the goaf’s upper corner.
4.5. Gas Analysis
A long-term field test was performed in the No. (9-15)06 panel using the comprehensive control method based on the gas sources. Overall, gas was adequately controlled. Figure 13 displays the monitoring of gas concentration in the panel during the working face mining. The gas concentration in the return airflow fluctuated within a range of 0.05% to 0.35%. The maximum gas concentration was no greater than 0.35%, below the early warning value of 0.5%.

5. Conclusions
Gas control has always been a key problem during slice mining of ultrathick coal seams with a high content of gas. This study examined the No. (9-15)06 panel with a mean thickness of 32.94 m in Liuhuanggou Coal Mine. The No. 9-15 coal seam included low-permeability ultrathick coal seams with a high content of gas. The No. (9-15)06 panel was the top-slicing working face of the No. 9-15 coal, using a fully mechanized top coal caving with a mining height of 9 m. A significant content of gas was emitted from the panel in the working face mining.
Based on the arrangement in the No. (9-15)06 panel and the surrounding mining condition, gas in the panel had four emission sources: from the coal wall, gas top coal caving, the goaf, and the neighboring coal seams. In this study, a comprehensive control method based on gas sources was proposed for the panel. Before the working face mining, gas emissions from the coal walls and top coal caving were lowered via gas predrainage alongside the coal seam. After the working face mining, gas accumulated in the caving and fracturing zones was drained using long-strike boreholes in the high-position drilling site. Drainage pipes were buried in the upper corner of the goaf to avoid gas accumulation emitted from destressed floor coal seams. During the working face mining, pressure-balancing ventilation caused the reduction of air leakage in the goaf and gas emission from the goaf.
Due to the great hardness and poor permeability of the No. 9-15 coal seam, conventional gas predrainage methods were not properly performed on the coal seam. Using hydraulic fracturing caused the enhancement of the permeability in the coal seam. Also, the backward-segmented technology was designed for improving hydraulic fracturing performance. To validate the superiority of the proposed method, the prefracturing performance of the coal seam was evaluated using borescope examination and gas emission test. Field test results demonstrated that the fractures can be developed in the coal seam around the boreholes after hydraulic fracturing. Fractures were mainly initiated radially from the borehole wall and then propagated in a spiral pattern consistent with crustal stress measurements. After the hydraulic fracturing, the mean gas predrainage was enhanced by four times.
Finally, a long-term field test was performed in the No. 9-15 panel to validate the superiority of the proposed comprehensive control method based on the gas sources. Long-term monitoring results indicated that the gas concentration in the return airflow fluctuates within a range of 0.05%~0.35%. No warning of excessive gas appeared in the panel. An adequate gas control can effectively ensure mining safety in the panel.
Data Availability
The data used to support the findings of this study are available from the corresponding authors upon request.
Conflicts of Interest
The authors declare no conflicts of interest.
Acknowledgments
This research is supported by the Natural Science Foundation of China (52004144), Natural Science Foundation of Shandong Province, China (ZR2019BEE001, ZR2018MEE009), and Key Research and Development Projects of Shandong Province, China (2019GSF111038). The authors thank the anonymous referees for their careful reading of this paper and valuable suggestions.